Apr 12, 2012 , by
Public Summary Month 4/2012
Technical problems related to the integration of the arm with the mobile base do not finish!
The arm lost its reference position and performed movements totally not coherent with the desired trajectories with strange mechanical noises. We called again technical assistance and they repaired the arm. The rest position is now correct. We are trying to implement the varnishing algorithms if any other technical problems do not arise.
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